commit 74402055a2d3ec998a1ded599e86185a27d9bbf4 upstream.
The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at time.
This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz
Fixes: 687c27676151 ("ARM: dts: Add minimal support for LogicPD Torpedo DM3730 devkit")
For linux-4.4.y
Signed-off-by: Adam Ford aford173@gmail.com
diff --git a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi index 80f6c78..e056704 100644 --- a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi +++ b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi @@ -90,6 +90,8 @@ };
&i2c1 { + pinctrl-names = "default"; + pinctrl-0 = <&i2c1_pins>; clock-frequency = <2600000>;
twl: twl@48 { @@ -137,6 +139,12 @@ OMAP3_CORE1_IOPAD(0x218e, PIN_OUTPUT | MUX_MODE4) /* mcbsp1_fsr.gpio_157 */ >; }; + i2c1_pins: pinmux_i2c1_pins { + pinctrl-single,pins = < + OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */ + OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */ + >; + }; };
&omap3_pmx_core2 {
On Mon, Mar 19, 2018 at 07:38:28AM -0500, Adam Ford wrote:
commit 74402055a2d3ec998a1ded599e86185a27d9bbf4 upstream.
The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at time.
This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz
Fixes: 687c27676151 ("ARM: dts: Add minimal support for LogicPD Torpedo DM3730 devkit")
For linux-4.4.y
Thanks, now applied.
greg k-h
linux-stable-mirror@lists.linaro.org